Last year I had a 24 volt 70 lb. Minnkota PD with auto pilot & us1 and it worked great. Because I planned to upgrade the depthfinder up front I sold it and got a refurbished motor from Fish Lectronics only its a V2 with us2. Because of knee issues I wasn’t able to get out until last Saturday. Well it didn’t go so well.The motor would run for 30 seconds and shut off. I had to unplug the unit and plug it back in to get it to work again for another 30 seconds. I did this about 5 times and called it quits and went back home. These are the same batteries and connections as last year. The batteries were fully charged as I let the onboard charger run all night. I checked the battery guage on the motor and it showed full charge. Put a volt meter in the plug in and it read 24.9 volts. Called Fish Lectronics and got it in. They ran it for 1/2 an hour at full speed without any problems. Tonight I disconnected the jumper on the batteries and had a friend do a load test on each of trolling motor batteries and they were fine. Reconnected the jumper and rechecked the plug in and it was at 24.9 v. With the volt meter plugged into the motor plugin we jiggled the wires to see if there was a loose connection and they are fine. I am stumped and upset. I’m going to Canada next Friday and am supposed to take my boat, but I’ve got to figure this out first. The only thing I can think of is maybe with the us2 plugged in, could that be causing it? I’m going to call FE in the morning and ask them if they hooked up a sonar unit to it when the ran it. That is the only thing I can think of that might be different from when I ran it.
Any help or suggestions would be greatly appreciated.
May 29, 2009 at 2:24 am
#1263067